Saudi Chiller Commissioning

Man commissioning a chiller in Saudi wareing head gear

Saudi Chiller Commissioning

We arranged the trip to carry out Saudi chiller commissioning for our Company Director and overseas engineer Dave Thompson. 2x 500kw air cooled chillers had been positioned at high level on a gantry. These were at the back of a newly constructed building at a factory in Jeddah. The factory produces plastic water pipes used for buildings and industry. Their own pipework, produced onsite, was used for the water systems of the plant in this article.

Water System Check Valves

There are two underground water system reservoirs for the plant. A check valve is fitted below the water line on the inlet pipe feeding all of the pumps. This ensures that water is available to the pumps on start up, despite the reservoirs being below the pumps.

Saudi Chiller Commissioning of Chiller Pump Set

The chiller pump set sucks water from the underground chiller reservoir. It then discharges the water through a plate heat exchanger, then it flows up to the chillers. The chilled water then returns 5°C cooler back to the underground chiller reservoir.

Saudi Chiller Commissioning of PHE Pump Set

Another pump set sucks from the separate underground process reservoir and discharges through the other side of the above mentioned plate heat exchanger. The water is chilled by around 5°C which can be adjusted with a pressure regulating valve on the outlet of the PHE. This chilled water then returns to the underground process reservoir.

Saudi Chiller Commissioning of Process Pump Set

A third pump set also sucks from the above mentioned underground process reservoir. It then discharges up to a ring main which goes along the top of 6 lines. Then, it drains down into plastic extrusion moulding machines to cool the newly formed plastic pipe. It does this at just the right rate to prevent bending and distortion. After this, the chilled water drains at gravity pressure back into the underground process reservoir.

0161 370 7193

service@maximuschillers.com

Contact Form

Control Panels for Pump Inverters

All of the pumps run on inverter drives which saves a significant amount of electricity. These drives are located in three panels- one for each pump set. A spare inverter is available in each panel for easy switch over in the event of failure. A touch screen pump control display is fitted to each panel. Each display is wired into a PLC.

Touch Screen Central Control

The PLCs in each panel are in turn wired into a Schneider Electric touch screen central control interface. This is located on the front of the middle panel. All of the analogue sensor and transducer inputs are wired into this interface from around the plant. The underground process reservoir temperature sensor was found to be reading 4°C high, so an offset was put into the program. The digital outputs go from here to the various components around the plant.

3 Way Valve

One of these components is a 3 way valve on the plate heat exchanger. This valve regulates the percentage flow of water through the PHE, relative to the percentage of bypass to the chillers. In high load conditions, 100% of water is pumped through the PHE. With no load, 0% of water goes through the PHE with full bypass to the chillers. In a low load condition, the valve modulates at between 0% and 100%. All of these scenarios achieve a close control of 20°C in the underground process reservoir.

Saudi Chiller Commissioning of Filtration Systems

Chiller Evaporators

The chiller evaporators are protected by a ‘y’ strainer on each inlet.

PHE Chiller Side

The plate heat exchanger also keeps contaminants from the process reaching the evaporators of the chillers. This prevents the premature failure of the evaporators and also prevents heat exchange issues due to thermal insulation.

PHE and Process Bollfilter

Both of these water systems go through a Bollfilter back flush system. As the difference in pressure between filter inlet and outlet reaches a predetermined level, the back flushing operation is initiated with a green light being illuminated. This feature prevents the need to manually clean the filter at scheduled intervals. During the visit, however, these filters were overwhelmed by the residue left in the pipes and a narrow 100 micron filter size. The maximum difference in pressure was exceeded and the filtration system yellow warning light became illuminated. The filters were stripped down, cleaned and reassembled.

‘Y’ Strainer in Parallel

The factory engineer who had designed the system had the foresight to build a second filter into the water system. This ‘y’ strainer runs in parallel to the above Bollfilter and ensures seamless operation of the factory in the event of a blocked Bollfilter.

0161 370 7193

service@maximuschillers.com

Contact Form

Start Up during Saudi Chiller Commissioning

On first start up of the chillers, they were both found to be tripping on high pressure and not loading up. The chillers run on R134a which is a low pressure refrigerant in the UK. In Saudi Arabia, however, the ambient is around 40°C. This translates to an operating pressure of between 15 bar and 18 bar depending on loading and water temperature.

Loading Solenoids

Unloader switches are available on each system. These feed back to the PLC, from here the program energises the loading solenoids. They had been set to 14 bar which was the cause of the unloading issue. Our overseas engineer set the switches to 19 bar.

High Pressure Switches

He then changed the high pressure cut outs from 15 bar to 20 bar.

PRVs Checked during Saudi Chiller Commissioning

The pressure relief valves vent at 23 bar which is enough of a difference in pressure from the high pressure cut out.

Low Load Trips

Because only one line was running at the time of commissioning, one of the chillers was found to have tripped on a low temperature related trip. This fault had occurred the following morning when the water temperature had become too low due to the minimum run time of the compressors. The freeze up set point was also found to be too high at 7°C. Our overseas engineer entered a password into the front end of each chiller and modified the parameters to prevent this fault re occurring.

Full Load Testing

The water system temperature was allowed to build up to 30°C when production in the factory was offline. Then, the chillers were ran in anger until set point was achieved. An efficient superheat value of 3°C was recorded on all of the systems. This is due to electronic expansion valves being fitted. When the factory came back online, the systems were found to be off cycling or unloading to match the load.

Chiller Redundancy

Redundancy has been considered in the capacity of the chillers to allow for future factory expansion and systems being offline during repairs.

Related Articles:
Global Chilled Water System Service

To read more about chiller control systems hit the Tag at the top of the page.

Read more about Jeddah on Wikipedia | Click Here


Two large air cooled chillers during condenser testing

Air Cooled Chiller Condenser Testing

We at Maximus Chillers have recently carried out air cooled chiller condenser testing at a new 3 year maintenance contract in the North West. The last of 4 systems had gone down on the morning that we first attended site. 1.2 MW of cooling had been lost which resulted in the water system temperature rising to 31°C. These chillers are used to cool an office block, so we wanted to get some of the systems up and running as quickly as possible…

News Article No.16

Air Cooled Chiller Condenser 1 Testing

One of the systems was disabled due to a condenser fan failure. 1 of 5 fans was found to be seized and disconnected. Fan speeds have sufficient redundancy built in to allow for a high ambient and a partially blocked condenser. There was a high ambient condition, but the condenser was found to be clean. Therefore, our engineer decided to run test the system and monitor the condenser pressure…

Fan Speed Transformer

3 fan speeds available on this chiller- low, medium and high. The fan speeds are achieved using a transformer which makes a different voltage for each fan speed. This is quite a good way of controlling the condenser pressure, as all of the fans run smoothly together. The program looks at the condenser pressure using a transducer, then selects the required fan speed.

Medium Fan Speed

As expected, the chiller program selected the medium fan speed. This provided the required saturation pressure in the condenser and so adequately subcooling the refrigerant.

Compressor Protection

All of the system pressures and temperatures were nominal, so the compressor was protected. There was a good oil return and sufficient cooling to the suction housing from the refrigerant. This cooling ensured that the internal motor windings did not overheat.

Monitoring

Having got this system away- our engineer monitored the water system temperature which started to come down. More cooling was required, however, to get the water system temperature down to set point…

0161 370 7193

service@maximuschillers.com

Contact Form

Air Cooled Chiller Condenser 2 Testing

Another system had been the only system running for some time.

Blocked Condenser

Grass pollination had caused a covering of organic material to accumulate on the condenser. The increased head pressure had caused the high pressure switch to trip. This type of material was easy for our apprentice to remove, as it clumped together when brushed.

HP Reset

The high pressure switch was reset and the system was run tested. It did not trip again, but a high pressure condition still persisted in the condenser.

Chemical Clean

Therefore, our engineer decided to carry out a chemical clean. After the whole of the ‘v’ type condenser was cleaned- the pressure came down a little.

Non Condensables

This system stayed running, but in the high fan speed. On the upcoming maintenance visit, a refrigerant diagnosis will be carried out to assess whether there are non condensables in the system. If this is the case, a false reading of subcooling will be recorded, as the non condensables throw out the calculation.

Cool Building

With 2 systems now running, the water system got down to set point. Our customer was really happy as the situation had gone from: office workers walking out of the building- to a cool building before 10 o’ clock on the first day of the contract.

Air Cooled Chiller Condenser 3 Testing

The third system had been on pressure test for the past 2 months with the condenser valved off. There was still pressure in the system, but our engineer decided to confirm the pressure test for himself. He did this by leaving it on pressure while having a drive round the suppliers. Several hours later, the pressure had remained constant, so he was able to start the evacuation process. After this was completed, the system was recharged and run tested. Now there were 3 systems up and running.

0161 370 7193

service@maximuschillers.com

Contact Form

Air Cooled Chiller Condenser PRV Testing

The pressure relief valves on the condensers have recently been changed. Industry guidelines state that they should be tested or replaced every 5 years. There is no guarantee that the PRVs will re seal satisfactorily after they have been tested. Therefore, in practice they are usually replaced. We inspected the date of the replacement, the burst pressure, the associated certification and paperwork- all was found to be satisfactory.

Air Cooled Chiller Condenser 4 Testing

The fourth system has a leak on the condenser with some refrigerant remaining in the system. This refrigerant will need to be decanted on a subsequent visit using a pump out unit and a recovery cylinder.

F-gas Leak Testing

The entire system will be pressure leak tested to identify the location of all leaks. Then, the leaks will be repaired using oxy-acetylene. After this, the system will be pressure tested to ensure its integrity.

Dehydration

Then, the dehydration process will be carried out. The achievable pressure of the vacuum pump will be tested and recorded. Evacuation will be carried out until this recorded pressure is achieved. Our engineers are issued with a powerful 10 cfm vacuum pump to speed up this process. This system will then be recharged and its operation tested.

Air Cooled Chiller Condenser Testing and Calibration

One of many tests that we will carry out on the upcoming maintenance visit is condenser transducer calibration. Transducer readings are not linear, so care will be taken to achieve an accurate calibration. A password will be entered into the controller to gain access to the required menu. Then, each of the transducers will be adjusted. The result of this means that accurate diagnosis can be carried out and the correct subcooling readings can be recorded.

The above is just part of the service that we provide to you- the customer! Having the capability to do anything and to extend the life of your chillers is part of what we call the MAXIMUS ADVANTAGE™ Any Chiller- Any Problem- Any Part- Any Refrigerant- Anywhere.

Related Articles:
Chilling Plant Service

Chilled Water System EEV Service

Water System Service of Evaporator

HFC Chiller Service

Process Chiller Vacuum Service

Chiller Breakdown

F-gas Chiller Leak Testing

Chiller Fault Finding & Diagnosis

To read more about air cooled chiller condensers hit the Tag at the top of the page.

Read more about pressure sensors on Wikipedia | Click Here


Boxed, shell and tube chiller condenser being lifted into a building with a crane

Chiller Condensers

Shell & Tube

The chiller condenser on a 2 MW centrif we look after had deteriorated over a long period of time. We had carried out tube cleaning and noticed that it had been extensively repaired in the past. There were a lot of damaged tubes that had been blanked off. This had reduced the useful surface area for heat exchange to occur. The chiller was experiencing a ‘discharge limiting’ condition which was causing it to back off to 54% capacity.

Air Cooled

Because of the difficulty to remove and replace the condenser from the plant room, the customer had explored the possibility of air cooled condensers. His idea was to fit the discharge and liquid piping up the side of the building and into the plant room. After considering this possibility, we decided to advise him against using air cooled condensers because it would take two, 16 fan ‘V’ types. This would have a footprint too big for the available space. We decided to use a crane to lift out the old condenser, then lift in the new one.

Pump Out

The old condenser was valved off from the rest of the system and the refrigerant was pumped into an 800 kg recovery vessel. This was one of 2 vessels in the plant room that had been there since the chiller was new.

0161 370 7193

service@maximuschillers.com

Contact Form

Lift Out for Chiller Condensers

The pipework was unbolted and the ancillaries removed. When it came to unbolting the condenser, some of the bolts were seized due to a long period of rusting. Some of them came loose by heating them with oxy-acetylene, the others were ground off with an angle grinder. We used a specialist lifting company to shift the condenser from the plant room and out to the lifting bay. They then attached slings to one end, manoeuvred that end of the condenser to the outside of the building, then attached slings to the other end. Rather them than me! Quite a dangerous operation, but it had been assessed when composing their Risk Assessment Method Statement. The condenser was lifted onto the back of an articulated truck and taken to a scrap yard for recycling. There was quite a lot of copper inside- so our customer got quite a good weigh in!

Lift In for Chiller Condensers

The new condenser, in the photo, was kept in its packaging during the lift up, so as to protect it from damage. Once it was in the building and near to the plant room, it was removed from the box and shifted the rest of the way with dollies. There was some difficulty getting it into its final location. This was because the old steelwork had to be cut back with a blow torch to make the new condenser fit. Also, with limited room and no gantry crane, the lifting company had their work cut out to manoeuvre it. Eventually, it was in location and we decided to call it a day.

Adapting the Pipework

This particular condenser was selected because it was similar in dimensions to the old one. The positioning of the refrigerant and water system pipework was similar too. That said, it was not an exact match. We called an industrial plumbing and welding company in to make the changes we needed. They measured up and built adaptors to bolt in between the condenser and the water system pipework. They cut back the new condenser discharge connection and welded a new flange on. This was so it could be bolted onto the existing discharge elbow from the chiller. The liquid pipe connection on the new condenser was in the same location, but came with a different thread. Therefore, this too was cut back and an adaptor fitting was welded into place.

0161 370 7193

service@maximuschillers.com

Contact Form

Ancillaries

The fittings on the new condenser were BSP and the fittings on the chiller were Flare. We carry an extensive range of fittings that go between BSP and Flare. We can go from male to female, female to male, male to male and female to female. We can step up and step down in size too. Using these fittings, we attached the high pressure switch and high pressure transducer. The wires for the liquid and discharge temperature sensors were extended. This was so they could reach the location of the pockets that were built into the new condenser. Then, we used a special heat transfer paste to get a good transmission of heat in between the sensors and the pockets.

F-gas Pressure Test

We then carried out a strength test and a pressure test in accordance with F-gas guidelines. This was witnessed at the beginning and at the end by the customer. A satisfactory outcome was achieved, so on to the next phase of the job…

Dehydration of Chiller Condensers

We needed to dehydrate the system and remove the nitrogen that was used in the pressure test. This is because nitrogen is a non condensable which will affect system performance. Our powerful vacuum pump was set up, then we left it running overnight. A 1.5 Torr vacuum was achieved, which was the same pressure as when the Torr gauge was fitted directly on to the vacuum pump.

Open the Valves and Test

After removing the vacuum pump, the recovered refrigerant was pumped back in, then the discharge and liquid valves were opened back up. Then, our engineer had a good look round for leaks. I know it had just been pressure tested, but we think it’s always a good idea to check again. This done, the water system pumps were started and the water temperature showed at 23°C on the controller. The set point for the chilled water was 6°C so this warm water was helpful as it gave us plenty of load to carry out the testing. The chiller went through a timer and then started up. It loaded steadily up to 100% with no dramatics- splendid!

Related Articles:
Chiller Parts Supplier

Chiller Compressors

Air Cooled Chiller Condenser Maintenance

Shell & Tube Evaporator Maintenance

Screw Chiller Compressor Maintenance

Chiller Controls

Scroll Chiller Compressor Maintenance

Centrifugal Chiller Compressor Maintenance

Reciprocating Chiller Compressor Maintenance

Chiller Controls Company

To read more about chiller condenser systems hit the Tag at the top of the page.

Read more about chiller condensers on The Engineering Mindset | Click Here


Blue recovery unit with a grey recovery cylinder during a chiller breakdown

Chiller Breakdown

A rainy day for a chiller breakdown for our engineer in the North West.

News Article No.8

Electrical Faults during Chiller Breakdown

Our customer called us out because he was having electrical faults with the chiller. The power supply to part of the panel had gone down and he required our assistance. Our engineer found a blown fuse which he replaced and tested operation- it blew again. Using his multimeter, he followed the diagnosis though to an earth fault on the flow switch…

Water System Flow Switches

The flow switch vapour seal had failed allowing rain water to ingress. This caused an earth failure on the 240v control circuit, and so blowing the fuse. The customer raised an order forthwith and so our engineer replaced the flow switch with the stock from his car. Each of our engineers keeps a range of flow switches for a variety of applications…

Stainless Steel

Where water system chemicals are corrosive, we carry corrosion resistant flow switches. This type has a longer working life due to the use of stainless steel. They are more expensive due to the higher manufacturing costs, but they are worth the money as they are less likely to fail, causing a potential loss of production.

Outside Use

This was the type fitted by our engineer on site in this news article. It has been developed and tested across a range of adverse weather conditions including freezing conditions and heavy rain. The electrical and switching compartment is protected by a sealing gland to keep the weather out. A rubber ‘o’ ring provides the seal into this compartment.

Inside Use

Some applications have the flow switch located inside the building in the plant room with the control cable extending out to the chiller controls. Another configuration allows for the flow switch to trip out the building controls and so dropping out the run signal to the chiller. In either case there is no need for weather proofing. This kind of flow switch is cheaper due to the lower construction costs.

High Pressure

Some water systems operate at considerable pressure. Therefore, high pressure flow switches have been developed for this application. They are capable of preventing water ingressing from the water system and into the electrical and switching compartment.

Test and Adjustment

Our engineer carried out testing and adjustments to the flow switch to ensure that it ran reliably. He achieved this by monitoring the water system readings and measurements against the design specifications of the switch. When he got it to settle down, he replaced the fuse and ran tested the chiller...

0161 370 7193

service@maximuschillers.com

Contact Form

Condenser Fans

The condenser fans were not coming on at all at first and later only slowly. They are controlled by a fan speed controller which is sensitive to pressure. A minimum value of volts is supplied to the fans, so as to prevent stalling and over heating of the internal motor windings. The fans were found to be in good working order, so he decided to turn his attention to…

Pressure Temperature Relationship of Refrigerant

There was found to be a lower pressure and so a lower temperature in the condenser. After careful fault finding and diagnosis involving putting the pressures and temperatures into a calculator, our engineer decided that the chiller was running short of refrigerant. This is consistent with Charles’s Law of Constant Volume. It is one of the fundamental scientific principals of how a chiller works: the higher the pressure- the higher the temperature/ the lower the pressure- the lower the temperature.

Recovery Units for Refrigerant

After receiving a further order from our customer, we gave the go ahead to our engineer to use his recovery unit to decant the gas. The refrigerant is sucked into the unit using a small one cylinder reciprocating compressor. The compressor discharges into the on board condenser which is cooled by a fan. The subcooled refrigerant travels down a refrigerant hose which is connected to the recovery cylinder in the picture. After this process was complete, he started looking for a leak...

Leak Testing and Pressure Testing

The leak was identified on the flange for the expansion valve. This component was removed, cleaned with our in house refrigerant grade solvent, then the joint re made with a compound suitable for the temperature range of the component. After a satisfactory nitrogen pressure test, the evacuation process can begin…

0161 370 7193

service@maximuschillers.com

Contact Form

Refrigerant System Vac Pumps

Each of our engineers carry a high capacity vacuum pump of the highest quality. We believe in investing in state of the art equipment as this is part of how we provide the MAXIMUS ADVANTAGE™ Any Chiller- Any Problem- Any Part- Any Refrigerant- Anywhere. Good equipment makes the job go easy.

Vane Pump

The pump works by sucking vapour into the inlet port. A rotary vane system extracts the vapour and discharges it through the top of the pump module. Oil is used to lubricate the vanes that slide around the pump cylinder. The vanes are kept a tight fit against the cylinder with the use of springs. As our pumps are high capacity, an oil filter is fitted to the outlet with a gauze inside to catch any oil droplets.

Electric Motor

This motor fits onto the back of the vane pump module. It comes from the factory set to 240v, but we change the pins for the electrical connections to convert it for use with 110v. This is because customers and engineers demand the use of 110v as if is safer for use in the UK climate. The 110v plugs and extension cable are shrouded and weather resistant. Weather resistant does not mean weatherproof, so we take measures to limit the exposure to adverse weather conditions. The pump motor, however, is not weather resistant at all, so care is taken to locate it somewhere dry. After a long time running, the motor runs hot, so our engineers take readings and carry out adjustments to ensure that it stays within its nominal operating temperature range.

Oil Changes during Chiller Breakdown

The vac pump oil is changed before each use with our specialist grade, high quality oil. Contact our office for prices and delivery times. The manufacturer of the pump recommends these oil changes as moisture and impurities absorb into the oil and so reduce its performance, also the working like of the pump.

0161 370 7193

service@maximuschillers.com

Contact Form

Refrigerant System Evacuation

Having set up the vacuum pump, our engineer started the evacuation process.

Torr Gauges used During Chiller Breakdown

We use analogue Torr gauges as they are more reliable than digital ones. Also, they do not need batteries and it does not matter if they get wet. Our engineer attached the Torr gauge to a suitable part of the system with a refrigerant hose, ensuring that a good seal was made between the components with a sealing compound.

Fittings used during Chiller Breakdown

Fittings were used to get between the different thread types from the vac pump to the fridge system. Having warmed up the pump for half an hour he was ready to start the process.

Non Condensables Removed during Chiller Breakdown

One purpose of evacuation is to remove the gasses that will not condense such as nitrogen remaining in the system from pressure testing. Another non condensable is air that has entered the system from when the expansion valve was removed. These non condensables affect how a fridge system works according to Dalton’s Law of Partial Pressures: that all gasses in a vessel act as if they are on their own. The non condensables cause a higher head pressure in the condenser. When this pressure is added into our calculation- it throws out the sum and so gives a false reading of subcooling.

Dehydration during Chiller Breakdown

The other purpose of evacuation is to dehydrate the system. Water, as we know, has a boiling point of 100°C at sea level, which is 1bar absolute or 760 Torr. As you start to drop the pressure, so correspondingly, the boiling point also drops. For example, water boils at the top of Mount Everest at around 68°C. If we continue vacuuming a refrigerant system, eventually we can remove all moisture by dropping the pressure below the saturation point of water. This works even in the winter in UK ambient conditions. Moisture in the system causes system failures and malfunctions leading to expensive breakdowns.

Related Articles:
Chilling Plant Service

Chilled Water System EEV Service

Water System Service of Evaporator

HFC Chiller Service

Process Chiller Vacuum Service

Chiller Service Company

Industrial Chiller Service

Chiller Service Company Visit

Chiller Fault Finding & Diagnosis

F-gas Chiller Leak Testing

Chiller Commissioning

Air Cooled Chiller Condenser Testing

To read more about chiller condenser fans hit the Tag at the top of the page.

Read more about rotary vane pumps at Wikipedia | Click Here


Brazing equipment box and vibration eliminators during packaged chiller service

Packaged Chiller Service

Packaged chiller service due to a refrigerant leak, resulting in a trip out. This visit was to identify the leak and get the plant back online.

Leak Testing During Packaged Chiller Service

Nitrogen was added to the system to aid in the identification of the leak. All parts of the system were checked, including the removal of lagging around the couplings onto the evaporator. The leak was found on a poor quality ‘eliminator’ which had rubbed through on the evaporator.

Vibration Eliminators

We decided to fit high quality vibration eliminators- see picture. These are fitted one in the horizontal position and the other in the vertical. They absorb both directions of vibration, then they are clamped to the chiller frame.

Brazing During Packaged Chiller Service

The pipework brazing was carried out with all combustible materials being removed from the work location. A permit to work was opened with our engineer as the responsible person. A half hour fire watch was carried out on completion of works.

0161 370 7193

service@maximuschillers.com

Contact Form

Pressure Test During Packaged Chiller Service

The pressure testing was carried out using nitrogen. As nitrogen is an inert gas, it will not cause other potential risks to the chiller and other personnel. The pressure test was a pass, so the next phase of the job could be carried out…

Vacuum Pump

Each engineer carries a 10 cfm vacuum pump. This high capacity ensures a fast vacuum. The Torr gauge was fitted to the system and 2 Torr was pulled.

Refrigerant Saturation

In the cylinder, the saturation of R407c is 7 bar at 11°C The refrigerant in the cylinder is in its liquid phase with vapour on top.

Subcooling

On run testing the chiller, the subcooling value was found to be nominal at the industry standard level.

Superheat

The superheat was adjusted, little by little, with the charging of the refrigerant until a good value was achieved. This was tested across all loading conditions for the rest of the visit.

Related Articles:
Chilling Plant Service

Chilled Water System EEV Service

Water System Service of Evaporator

HFC Chiller Service

Process Chiller Vacuum Service

Chiller Service Company

Chiller Breakdown

Industrial Chiller Service

Chiller Service Company Visit

Chiller Fault Finding & Diagnosis

Read more about reducing refrigerant leaks at the Institute of Refrigeration | Click Here


Carel controller and tick sheet during chilling plant maintenance visit

Chilling Plant Maintenance Visit

On this chilling plant maintenance visit, particular attention was made to compressor loading. This was to ensure that the compressors are capable of operating at 100%. With summer now here- we want the plant capable of running at full capacity.

Controller Loading Timer

On start up, the controller goes through a timer, this is to prevent the compressor from loading up too quickly, achieving set point and going off. With available load, the compressor would start back up and go into a short cycling condition. With 5 minute intervals, the controller brings System 1 screw compressor on at 25%. Then System 2 screw compressor on at 25%. In stages, the controller loads up the compressors until it matches the load.

Compressor Loading Solenoid Coils

These are 24vac. The controller sends out a run signal through the solenoid coil which magnetises the lift valve inside.

0161 370 7193

service@maximuschillers.com

Contact Form

Compressor Loading Solenoid Valves

As the valve lifts, discharge pressure oil passes through a channel and pushes the slide valve open a 25% stage. There are 4 valves for the 4 stages.

Chilling Plant Maintenance Visit at 100%

The chilling plant being maintained on this visit was now running at 100% on both systems. The system readings can easily be read by following the menu in the Carrel controller. Superheat and subcooling readings were found to be within normal operating limits. Also, a good read back was recorded on the water system.

Compressor Unloading

At the end of the day, the three way valves on the air handlers closed down according to the BMS schedule. This meant that the water was diverted away from the heat exchangers in the air handlers. This return water had not picked up any heat, so the controller started unloading the compressors. It did this through 75% to 50% then 25% until the water system was down to setpoint.

Off Cycle at Chilling Plant Maintenance Visit

The BMS stops the chiller with the remote start/ stop signal. Should the BMS malfunction, the chiller would stay off most of the night anyway. The water system pump adds heat into the water system. Therefore, every so often enough load would be available to bring one system on at 25% for a short while.

To read more about chiller compressor systems click the Tag at the top of the page.

Related Articles:
Air Cooled Chiller Planned Maintenance

Water Chiller Maintenance

Process Chiller Maintenance Visit

Chilled Water System Maintenance

Centrifugal Chiller Maintenance

Industrial Chiller Maintenance

Chilling Plant Controls Maintenance

R134a Chilling Plant Maintenance

Chiller Maintenance Checklist

Glycol Chiller Maintenance

Read all about solenoid valves on Wikipedia | Click Here


Process chiller maintenance of grey Italian chiller with cover removed

Process Chiller Maintenance

Maximus Chillers recently carried out process chiller maintenance to an Italian machine.

Process Chiller Maintenance for Water Level Sensor

The process chiller has a water treatment schedule, but the water level sensor needed maintenance. This is because the three probes of the sensor were not completing continuity. The probes complete the continuity from the wire going into the sensor, along the probe, then to another wire back to the controls of the chiller.

Low Water Probe

If the controls loose continuity to the low water probe, the alarm is triggered and a call out is arranged to resolve the issue.

Correct Level Probe

In normal operation, the correct level probe is activated and the chiller runs as normal.

High Water Level Probe

Should the high water level probe be activated, again the alarm is triggered and a call out arranged.

0161 370 7193

service@maximuschillers.com

Contact Form

Process Chiller Maintenance Call Out

As we were already on site to carry out the maintenance, there was no need to arrange a call out. We soaked the sensor for an hour in a special a decontamination chemical that has been designed to restore the probes. That done, the rest of the maintenance was carried out including the tightening of the wiring and motor connectors. It was possible to do this on this visit as the factory was not in production.

Run Testing

All readings around the chiller were taken when the factory went back into production. We found the fridge system to be working with optimum efficiency, meaning that the chiller will use the optimum amount of electricity. Efficiency is a great concern to a factory as they want to reduce their carbon footprint as much as possible.

Related Articles:
R134a Chilling Plant Maintenance

Water Chiller Maintenance

Air Cooled Chiller Planned Maintenance

Chilled Water System Maintenance

Centrifugal Chiller Maintenance

Industrial Chiller Maintenance

Air Cooled Chiller Condenser Maintenance

Chiller Maintenance Checklist

Planned Preventative Chiller Maintenance

Chiller Maintenance Schedule

Air Cooled Chiller Maintenance

Chiller Maintenance Company

Chilling Plant Maintenance

Preventative Chiller Maintenance

Follow this link for the IOR celebration of chiller service engineers Click Here


Mirror looking for leak during chilled water system eev service

Chilled Water System EEV Service

Chilled water system EEV service was being carried out because the mechanical parts had failed. This particular valve is prone to this fault. It is an OEM electronic expansion valve, so our technician found the voltage for the motor and found a similar part with the same amount of steps.

The EEV driver was found to be functioning satisfactorily. Sometimes, depending on how the mechanical part of the EEV has failed, the driver can be overloaded and burned out.

Electronic Component Refurbishment

Where electronic parts, such as the EEV driver, are found to be burned out- Maximus Chillers has a refurbishment laboratory at head office. We have the capability to strip down the component and fault find where it has blown. Usually it is quite simple: the jammed mechanical part of the valve has burned out the motor for example. More complex fault finding and component replacement on the circuit board can be carried out also. Another option is to replace the driver with a like for like swap or retrofit to a different driver.

0161 370 7193

service@maximuschillers.com

Contact Form

Pump Down for Chilled Water System EEV Service

The chiller was pumped down and valved off. This saves on the time and recovery vessel to pump the refrigerant out.

Remove and Replace

Once pumped down, our engineer removed and replaced the valve, sealing it on its knife edge seal. The wire was passed up the conduit and into the panel. The wiring colour scheme was different on the new valve, so some time was taken to ensure it was wired up correctly.

Restart after Chilled Water System EEV Service

After leak testing, the refrigerant system valves were opened back up and the plant switched back on. The correct superheat and subcooling values were achieved concluding a successful visit.

Related Articles:
Chilling Plant Service

Water System Service of Evaporator

Process Chiller Service

Chiller Fan Deck Service

Packaged Chiller Service

HFC Chiller Service

Process Chiller Vacuum Service

Chiller Service Company

Chiller Breakdown

Industrial Chiller Service

Chiller Service Company Visit

Chiller Fault Finding & Diagnosis

F-gas Chiller Leak Testing

Chiller Commissioning

To read the Institute of Refrigeration guide to expansion valves | Click Here


Industrial refrigeration oil change showing ammonia warning sign

Industrial Refrigeration Oil

An industrial refrigeration oil visit was arranged because of a return issue. Several fans had been down on the air cooled system. This causes the system to unload so as to prevent a fault occurring. The lower mass flow rate of the refrigerant caused oil to migrate to the low side of the system. Several vessels are available with various forms oil return. These vessels and the oil cooler were valved off. A two man team with the correct ammonia PPE and breathing apparatus carried out the job.

Industrial Refrigeration Oil Recovery

Only some of the oil was recovered from the plant. Therefore, the engineers decided to add new oil to get the system running. The only problem with doing this is that once running the machine, the oil has to be got back out. Therefore, the oil had to be adjusted a second time to resolve the oil return issue.

0161 370 7193

service@maximuschillers.com

Contact Form

Fan Decks

For this visit, scaffolding had been erected in accordance with the Risk Assessment. The old fan decks were lifted out by the two man team. A really good team was sent out: one of the men was more technical and the other more mechanical- complementing each other with their different skill sets. The new fans were an updated version and the wiring was different. The fault link had to be adapted, but the 0-10v input from the controller was the same. The controller reads the pressure from a transducer, then sends out a voltage which the fan turns into the corresponding speed.

System Testing

The fault link had been correctly modified, so the testing of the system was carried out. The machine loaded up to 62% and monitoring continued during the rest of the visit.

Any Chiller- Any Problem- Any Part- Any Refrigerant- Anywhere- The MAXIMUS ADVANTAGE™

Related Articles:
Industrial Refrigeration Sludge

Industrial Refrigeration Ammonia

Read More about International Institute of Ammonia Refrigeration Technology and Standards.

 


Translate